Case Study Spotlight: Boiler Feed Pump 1B – Misalignment of Booster Pump (Jan 2011)
How vibration trending, 1× spectrum, and phase analysis confirmed
misalignment—and how simple mechanical fixes restored stable operation.
Why this
matters
Boiler feed pumps (BFPs) are among the most critical
auxiliaries in a thermal power station because they deliver feedwater to the
boiler at high pressure. Loss of a BFP can quickly become a generation risk if
standby redundancy is compromised. This case study shows how condition
monitoring detected a developing problem early, confirmed the fault mechanism,
and validated the repair.
1)
Background and initial symptoms
After planned servicing during a unit overhaul in December
2010, routine vibration monitoring identified an abnormal rise in horizontal
velocity on the booster pump bearings. Importantly, the motor, hydraulic
coupling, and main pump vibration levels remained normal, and operating
parameters such as pressure and temperature were also normal. Because the
vibration trend continued to increase, the team decided to change over the pump
for inspection.
Key
observations (pre-maintenance)
·
Horizontal velocity at booster pump DE and NDE
increased from typical values to 4.8 and 4.1 mm/s RMS, respectively, and later
reached 5.9 mm/s RMS at the DE.
·
The abnormality was localized to the booster
pump: other drive-group components showed normal vibration behavior.
2)
Diagnostic workflow (what the vibration data was telling us)
The team followed a simple but powerful sequence: (i)
confirm the trend change, (ii) look for the dominant spectral component, and
(iii) use phase to validate the fault type.
2.1 Trend +
overall levels
Overall velocity levels at the booster pump were
significantly elevated compared with the normal range (about 2.5–3.0 mm/s RMS),
prompting spectrum analysis.
2.2
Frequency domain (FFT spectrum)
Spectrum analysis showed a clear increase at 1× running
speed (around 1480 rpm). A dominant 1× component on a coupled machine train is
a classic indicator of alignment-related forcing, especially when it grows
without corresponding increases at bearing defect frequencies.
2.3 Phase
analysis (the clincher)
To confirm misalignment, phase across the coupling was
measured. A phase difference of approximately 180° across the coupling strongly
supported a misalignment condition between the booster pump and motor.
3) What was
found during maintenance
During decoupling and inspection, the bearings showed no
scoring and housings were acceptable. However, two mechanical contributors to
misalignment/instability were discovered:
·
Six flexible coupling bolts were found
sheared/damaged.
·
Foundation bolt shims below the suction strainer
were loose.
4)
Corrective actions (repair + alignment)
The corrective work focused on restoring mechanical
integrity and re-establishing precise alignment:
1. Decoupled
the booster pump from the drive group and recorded initial alignment readings
for reference.
2. Replaced
the sheared coupling bolts with new bolts.
3. Adjusted
shimming at the suction strainer (trial 5 mm shims at all four corners, then
refined to 4 mm shims) to achieve precise alignment and allow smooth expansion.
4. Completed
alignment of the booster pump with the rest of the drive group (dial gauge
method described in the case study) and performed a trial run; vibrations were
within limits.
5) Results
and verification
Post-maintenance measurements confirmed that vibration
returned to normal levels after bolt replacement and alignment work, and
post-maintenance spectra did not show misalignment/looseness indicators.
Selected
before/after vibration levels (velocity, mm/s RMS)
|
Component |
Point |
Direction |
30/12/2010 (Initial) |
03/01/2011 (After re-alignment) |
|
Booster pump |
DE |
H |
5.9 |
2.9 |
|
Booster pump |
DE |
V |
2.8 |
1.4 |
|
Booster pump |
DE |
A |
2.0 |
1.3 |
|
Booster pump |
NDE |
H |
4.1 |
2.5 |
|
Booster pump |
NDE |
V |
3.2 |
2.7 |
|
Booster pump |
NDE |
A |
1.2 |
1.1 |
6) What
this case teaches (practical takeaways)
·
Localize the fault: when one element in a drive
group deviates while others stay normal, focus diagnostics on that element and
its interface (coupling, base, soft-foot, shims).
·
Use phase to separate ‘looks like misalignment’
from ‘is misalignment’: a strong 1× peak plus ~180° coupling phase difference
is compelling evidence.
·
Inspect what the data is pointing to: coupling
hardware and base/shimming issues can turn an alignment problem into a
reliability risk quickly.
·
Always close the loop: the repair is not
complete until post-maintenance readings and spectra verify stability.
Business
impact (why condition monitoring pays)
By acting on the rising trend, confirming misalignment
through spectrum and phase analysis, and correcting the hardware/alignment
issues, the maintenance team restored the BFP to service with stable vibration.
The case study reports this proactive intervention helped avoid significant
losses and estimates the cost impact at approximately Rs. 73 lakhs (including
generation loss and associated maintenance costs).
Reference
Bari, H. and Thaker, J. (2025) Condition Monitoring in
Thermal Power Stations: Case Studies. 1st edn. Boca Raton, FL: CRC Press. DOI:
10.1201/9781003432616.
Figures
Note: Baseline value represents the typical operating range (approximately 2.5-3.0 mm/s RMS) noted in the case study; dates are shown for illustration based on the case timeline (late Dec 2010 to early Jan 2011).



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